| ORTHOPAEDIC FACTORY
OPENS FLOOD GATES ON ENERGY SAVING
October 2007
A factory’s
plan to save energy by upgrading from v-belts to timing belts
on air handling drives has been expanded to include a wide range
of automation equipment. This has cut Euro 140,000 from the annual
energy bill, improved the work environment and suggested further
savings.
Stryker
Orthopaedics manufacture a range of Orthopaedic implants, Bone
Cements and Bone Substitute Materials at it’s facility in
Limerick, Ireland. The facility has been in operation for over
35 years and employs 500 people. Like many other companies it
has become increasingly aware of energy cost increases in recent
years and has undertaken several initiatives to reduce energy
usage/costs and to protect the environment.
Late last
year, maintenance manager Robert McKillican calculated that changing
from v-belts to timing belts would reduce energy consumption by
about 10 percent and called in local industrial factor Michael
Dineen of Dickson Bearings to discuss the idea. But it was soon
realised that slippage of the v-belts gave a soft starting effect,
which would be lost with a toothed belt.
The two briefly
considered the use of electronic soft starts, but soon decided
that variable speed drives would be better because they could
be used to tune the air handling to exactly match demand.
Stryker’s
plant has eight extraction fans, all worked quite hard to ensure
complete extraction of dust particles. Initial calculations suggested
that significant energy savings could be made if each were tuned
to exact local demand, rather than run faster than necessary.
Additionally, staff numbers and production levels vary during
Stryker's two-shift day so there is potential to further slow
down the air handling at different times throughout the shifts.
There were
a number of practical issues to be addressed, not least which
drive to use.
Michael undertook
some research and recommended the L300P Series from Hitachi, three
at 55kW and five at 37kW, which are particularly appropriate for
fan drive applications and have an enviable track record on energy
saving applications.
Meanwhile
Robert was unearthing some practical considerations.
The control panels, for instance, had to be designed to fit into
a smaller than ideal control room. And they would be close to
some sensitive equipment, so chokes would be required on every
input and output to minimise noise generation and harmonics onto
the mains. With the Hitachi drives it was also possible to set
a maximum total output, so that penalty charges from the electricity
supplier could be avoided.
A PLC would
be required to control the system, and it seemed logical to stick
with Hitachi and use an EH150 series. This communicates with the
plant’s existing building management system (BMS) to make
the whole installation intelligent and interactive.
Finally it
was realised that security staff as well as control engineers
would need access to the system. It was decide therefore to install
two touch screen HMIs, again Hitachi, one in the control room
the other in the security office, and to use clear graphical displays
to make use as intuitive as possible.
Within days
of completing the installation, energy meters strategically located
around the system were confirming that considerable savings were
being made. No detrimental effect on machine performance or other
production compromises were identified. But Robert was not ready
to rest on his laurels; he knew that there were further improvements
to be made, although he had to introduce them slowly so that production
was never disrupted.
Initially
the drives were configured to give the fans three set speeds,
but the intention is to upgrade this with PID pressure sensor
feedback so that load matching becomes exact. With the PLC and
BMS working together, it has been possible to programme in timings
for tea- and lunch breaks so that the air handling is not running
unnecessarily when machines are idle for two hours each day.
Robert says
that there were other gains too: “Simply putting drives
into our system improved our electrical usage profile, so is saving
us an extra 15 percent above expectations.
“By
load matching we have eliminated draughts from around the shop
floor, so people are more comfortable due to the improved work
environment.
“But the biggest unexpected saving – and it is massive
- is in the gas bill for space heating. Not only are we pulling
in less outside air, but we are now able to recycle half of our
heated air. We are saving Euro60,000 on gas, nearly 30 percent,
and there is scope to further increase the recycling!” This
is on top of a €80,000 saving that has been made on electricity,
to run the dust extraction system.
With the bit
between his teeth Robert is now working on several more energy
saving projects. Motors throughout the site are being audited
for efficiency; lighting has been modernised, generating a Euro60,000
saving; those air handling units without recirculation capabilities
are being upgraded.
“We
have written a new module for our SCADA software so that we can
monitor energy consumption in each manufacturing cell. Soon each
machine manager will be accountable for his own measured energy
consumption; I expect this will lead to a significant change in
thinking and that a great multitude of minor energy losses will
be brought under strict control.
“For
many years we senior managers were able to ignore energy issues,
but once we started monitoring usage our attitude changed completely.
This is now filtering out to the whole workforce. And the lesson
is that monitoring energy consumption leads to a constant drive
for more savings.”
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